Quote Originally Posted by PetefromtheStreets View Post
Ok so it's been a while since I've been posting. I've had various reasons as to why that is. Mainly because I didn't want everyone knowing 100% of what my car had done on the dyno. But I just don't care anymore at this point.

So anyways I found out what my Ecu issue was. My kpro board had fried. So I sent my Ecu is for diag/repair. $350 later I received a working kpro.

Car started up perfect. THANK GOD!

Got the car loaded up on the trailer and off we went to the shop.



#treblictuned shop is the shit. Nothing in there that isn't racecar. Except mine when He pulled it on the dyno.




Strapped her down and he built me up a Kal. Asked me questions about the build, trans, wastegate, Ect.
He did his first pull to see what the gate would hold. It held a solid 6psi to redline


Car made like 240hp. That was pretty sweet. But even with the pwm booster the spring would only go to 9psi at 80% duty cycle. So we took the gate off and changed out the spring to a 12psi Spring. Going from 6psi spring to 12lb Spring the car picked up 100hp. Lol



Tuning in 93 pump gas from 7-11. The car layed down 554hp @ 17psi with the filter on the turbo. I asked him if the filter was too small and he said "let's do a pull with it off".



Car made 562hp with it off. So all in all the filter is doing pretty well. Flowing enough Ect.


Out goes the pump gas and in goes the race gas. 2- 5 gallons of Q16.


First pull on the gas with modified ignition car made 640hp tires barely holding the power to redline. Next pull he added to trackbite to the rollers to try and help and it blew the tires off and made 646hp.


Tuner said he was Leary about tuning in 4th gear as the car would pick up a shit ton of torque. He was worried about the trans. (He forgot I had a PPG do my box in there. Lol) so I said fuck that put it in 4th.

First pull In 4th gear 30psi a coupler blew off the tb and the car made an astounding 780whp.



I couldn't believe the car had just done that. My goal walking in there was 700. And 740 MAX! But it made that. I kept asking if that was real!

We fixed the coupler and used a bit of hairspray to keep it on this time. Next run on the dyno.



Made 793whp 603ft/lb trq @30.1psi.

My little Borg s366 was putting in some work.

We turned it back down to 27psi and it made 733whp. So that is where it sits currently.



All in all I am extremely happy with the car and tune and it's amazing how much power these K's can make. Only trouble being the chassis it's in. They are so heavy and restrictive.

I drove the car to the track the next weekend and got tires switched over.

Car looks mean AF!



First pass of the day

11.5 @ 139mph

Car drifted towards the wall and yes I got scared of it. Lol

2nd pass.
11.33 @ 122mph
Car drifted again and started cutting out. Let off at some point.

3rd pass
11.1 @ 143mph
Car ran solid but I knew it had more. I was getting more and more comfortable with it.

I decided I wasn't leaving till I went 10's.

So back to the lanes I went.

4th pass
10.74 @ 145
Car ran great. Small hiccup with the throttle.



Found out the tps wires were held on by a couple strands on one or two wires.

Fixed that and am about to head back to get some more personal bests.

Wish me luck.


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Awesome write up and results!! 10.7 @ 145 is great. Eager to see what happens next!!