I think I saw a pic of that on 8thcivic! Way better than the 3 bolt... They suck mad balls to stuck any tool to get them out of there.
I tried that but... no deal.
Spaz's solution worked... I wraped that portion of the exhaust with leftovers of my DEI wrap and over that I've put the cutted hoseHope it holds forever lol
Thanks! Better safe than sorry. Specially for the price of those studs...
After a while it's update time:
Came back to E100...
Put back on the 2200cc injectors,the brazilian LXS fpr (we measured 65 psi on that little bitch) and returned building boost slowly. At 12 psi the car started asking 10% fuel... But even adding fuel my lambda was at the same value and just the IDC was going up
Maybe the single DW300 can't handle the flow, or is it defective?
Well, our postal service was on strike (and guess what, they are the only one allowed to handle mail lol) and my return system will be delayed once more.
Dunno guys, but what do you think?
E100 flows approx. 45 - 50 % more than gas.
I was trying to go with only one pump as long as I could.
I also changed the fuel filter hoping that it was clogged, but that didn't do either.
Can't think about another thing than that the pump atm.






Hope it holds forever lol
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